首页 | 本学科首页   官方微博 | 高级检索  
     检索      

低渗透性煤层注液态CO2置换驱替CH4试验
引用本文:马砺,魏高明,王世斌,李珍宝,刘新民.低渗透性煤层注液态CO2置换驱替CH4试验[J].重庆大学学报(自然科学版),2018,41(6):76-83.
作者姓名:马砺  魏高明  王世斌  李珍宝  刘新民
作者单位:西安科技大学 西部矿井开采及灾害防治教育部重点实验室,西安710054;西安科技大学 安全与科学工程学院 ,西安710054 韩城矿务局 ,陕西韩城,715400
基金项目:国家自然科学基金资助项目(51574193
摘    要:针对低渗透性煤层瓦斯难以抽采的问题,结合液态CO_2低温、低黏、渗流阻力小、相变增压等特性,提出低渗透性煤层注液态CO_2置换驱替CH_4技术。在韩城矿区桑树坪二号井开展煤层注液态CO_2置换驱替CH_4工业性试验,开发了压注工艺系统,确定了压注关键性参数,判定了CO_2置换驱替CH_4技术效果。试验结果表明:液态CO_2压注时压力呈现波动特性,起始升压速率较快,达到2.5MPa左右时趋于稳定;压注管路瞬时流量为0.6~1.4m~3/h,累计压注液态CO_2为6.0m~3;以压注过程中检验孔内CO_2体积分数为指标,判定试验有效影响半径达到18m。试验区域瓦斯抽采体积分数是原始体积分数的2.5倍,抽采纯量是原始纯量的3.5倍,相比瓦斯抽采效率提高。

关 键 词:低渗透性煤层  液态CO2  影响半径  瓦斯抽采  置换驱替
收稿时间:2018/1/5 0:00:00

Experimental study of displacing & replacing methane in low permeability coal seam by injecting liquid carbon dioxide
MA Li,WEI Gaoming,WANG Shibin,LI Zhenbao and LIU Xinmin.Experimental study of displacing & replacing methane in low permeability coal seam by injecting liquid carbon dioxide[J].Journal of Chongqing University(Natural Science Edition),2018,41(6):76-83.
Authors:MA Li  WEI Gaoming  WANG Shibin  LI Zhenbao and LIU Xinmin
Institution:College of Energy Science & Engineering, Xi''an University of Science and Technology, Xi''an 710054, P. R. China;Key Laboratory for Coal Exploitation and Disaster Prevention under Ministry of Education, Xi''an University of Science and Technology, Xi''an 710054, P. R. China,College of Energy Science & Engineering, Xi''an University of Science and Technology, Xi''an 710054, P. R. China;Key Laboratory for Coal Exploitation and Disaster Prevention under Ministry of Education, Xi''an University of Science and Technology, Xi''an 710054, P. R. China,Hancheng Mining Bureau, Hangcheng 715400, Shaanxi, P. R. China,College of Energy Science & Engineering, Xi''an University of Science and Technology, Xi''an 710054, P. R. China;Key Laboratory for Coal Exploitation and Disaster Prevention under Ministry of Education, Xi''an University of Science and Technology, Xi''an 710054, P. R. China and Hancheng Mining Bureau, Hangcheng 715400, Shaanxi, P. R. China
Abstract:This paper is to solve the gas drainage problem of low permeability coal seam. Based on the characteristics of liquid carbon dioxide with low temperature, viscosity, percolation resistance and phase change pressurization, the liquid carbon dioxide enhanced methane recovery technology was proposed to improve the gas drainage efficiency. Liquid carbon dioxide injection test was carried out at Sangshuping No.2 mine shaft,Hancheng mining area, and by which injection process was developed, the key parameters were determined and the methane extraction efficiency influenced by carbon dioxide was examined. The results show that the pressure of injecting is fluctuated. Initially, injecting pressure rises fast and then keeps stable when rising to 2.5 MPa.The flow rate of injection maintains from 0.6 m3/h to 1.4 m3/h and the total cumulant of liquid carbon dioxide is 6.0 m3. The concentration of carbon dioxide in the test borehole is taken as index, and it''s found that the influence radius of the test is 18 m. The methane concentration and the purity in the test area are 2.5 and 3.5 times of those in the original data respectively, which proves the proposed technology enhances the gas extraction efficiency.
Keywords:low permeabilitycoal seam  liquid carbon dioxide  influence radius  gas extraction  displacement and replacement
本文献已被 CNKI 万方数据 等数据库收录!
点击此处可从《重庆大学学报(自然科学版)》浏览原始摘要信息
点击此处可从《重庆大学学报(自然科学版)》下载免费的PDF全文
设为首页 | 免责声明 | 关于勤云 | 加入收藏

Copyright©北京勤云科技发展有限公司  京ICP备09084417号