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连续油管冲砂解堵在水平井中的应用
引用本文:俞宏伟,姜一超.连续油管冲砂解堵在水平井中的应用[J].科学技术与工程,2011,11(32).
作者姓名:俞宏伟  姜一超
作者单位:1. 提高石油采收率国家重点实验室,中国石油勘探开发研究院,北京 100083
2. 中国石油华北油田公司采油五厂
摘    要:冀东油田G104区块拥有水平井110多口,油藏岩石颗粒胶结疏松,出砂严重;原油属普通稠油,胶质沥青质含量高,凝固点低,导致了水平井筛管段严重堵塞及近井地带导流能力的下降,直接影响了产量。只能依靠除砂、解堵技术来恢复该区的产量。针对该问题,采用外径4.45cm连续油管 RotoPulseSM旋转脉冲喷射工具 一步酸、半加强型砂盐酸体系进行冲砂、筛管清洗和近井酸化解堵对该区6口水平井实施了作业。作业后产液量和产油量是作业前的1.8倍以上,作业有效期超过200天,增产效果明显。

关 键 词:水平井  连续油管  冲砂解堵  受力分析
收稿时间:8/29/2011 4:25:44 PM
修稿时间:9/2/2011 6:05:59 PM

APPLICATION OF COILED TUBING SAND WASHING AND FLUSHING TECHNOLOGY IN HORIZONTAL WELL
yuhongwei and jiangyichao.APPLICATION OF COILED TUBING SAND WASHING AND FLUSHING TECHNOLOGY IN HORIZONTAL WELL[J].Science Technology and Engineering,2011,11(32).
Authors:yuhongwei and jiangyichao
Institution:The Fifth Exploit Factory of Huabei Oilfield Company, PetroChina
Abstract:The cementation of rock particles in G104 block of Jidong oil field is loose, and much sand has been entering the well bore. The oil is heavy, gum and asphaltenes content is high, and the freezing point is low, which leads to the blocking up of screen pipe and depression of flow conductivity around the well bore, affecting the production directly. The operation used 1 3/4" coiled tubing RotoPulseSM tools one shot acid and 1/2 strength sandstone acid on 6 horizontal wells to solve this problem. After the operation the production of fluid and oil in this 6 wells are all about 0.8 times more than that of before.
Keywords:coiled tubing  sand washing and flushing  horizontal well  force analysis
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