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滨南油田低渗欠注井酸化增注技术研究与应用
引用本文:朱桂林,李根生.滨南油田低渗欠注井酸化增注技术研究与应用[J].中国石油大学学报(自然科学版),2003,27(2).
作者姓名:朱桂林  李根生
作者单位:1. 胜利油田有限公司滨南采油厂,山东,东营,257000
2. 石油大学石油工程学院,山东,东营,257061
基金项目:中国石化集团公司重点科技项目 (P0 10 3 1)
摘    要:提出了一种针对滨南低渗油田欠注井酸化增注的系统实验研究方法。根据储层特征分析了注污水和重复酸化对地层的损害及对酸化液的选取原则。根据长岩心酸化流动模拟实验进行了酸化工艺参数优选及其评估分析。现场施工证明该酸化液体系适应性较好 ,工艺参数合理 ,能够较好地解除地层中有机物和无机物堵塞 ,提高注水量 ,降低泵注压力 ,在低渗油田注水井中具有推广价值。

关 键 词:滨南油田  低渗油田  欠注井  砂岩基质酸化  长岩心流动模拟实验

Application of acidizing and augmented injection technology to injection wells in low-permeability reservoir of Binnan oil field
ZHU Gui lin and LI Gen sheng. Binnan Production Plant of Shengli Oil Field Corporation Limited,Dongying.Application of acidizing and augmented injection technology to injection wells in low-permeability reservoir of Binnan oil field[J].Journal of China University of Petroleum,2003,27(2).
Authors:ZHU Gui lin and LI Gen sheng Binnan Production Plant of Shengli Oil Field Corporation Limited  Dongying
Institution:ZHU Gui lin and LI Gen sheng. Binnan Production Plant of Shengli Oil Field Corporation Limited,Dongying 257000
Abstract:A systematical experimental method of acid treatment for increasing injection of injection wells and well stimulation in the low permeability reservoir of Binnan oil field was proposed. The reservoir performance before acid treatment, the formation damage resulted from injection of polluted water and acidization for many times, as well as the selection principles for different types of acids were discussed. The simulation experiments on the long core flow were carried out. The acidizing parameters on the spot were optimized and evaluated. The practice demonstrated that the acid system obtained from the laboratory test and the parameters adopted on the oil field are suitable for removing plugging and increase the injection of water in the low permeability wells. This method can be generalized in the water injection wells with low\|permeability.
Keywords:Binnan oil field  low  permeability reservoir  under injection wells  sandstone matrix acidizing  long core fluid flow simulation test
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